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journal/stockcropper/Untitled 1.md

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Jack nut pressed in really tight. Loosen this a bit if at all possible. It made the threads jam up. I re-tapped the threads after pressing it in. It didnt press in all the way (about 1/16” didnt go in) but the flange also wasnt quite to spec so this is a good representation.
Everything went on the axle tighter than desired. Maybe this should be undersized.
The main axle is too long for the pins to latch over. I think it was fabricated wrong… double check this. We just elongated the clips on the pins for now.
I sanded out the bores for the main axle bushings. This didnt take long. This is probably the right thing to do - dont even change the nominal hole size, just sand to a nice tight slip fit.
The main tube would go on easier if it just bottomed out against the bushing. Just do it. Or slot the sheetmetal. Do something so this is easy.
Maybe you should make the towbar telescope!
The drive motor purchased had M8 threads. It also didnt need the spacers (spacing was perfect already!). It just needed the shaft cut down. Verify what youre working with.
Need to chase / retap the M12x1 nuts after welding (and prior to painting).
You didnt order or make the steering handle. Robbed part from THF. Its not the right thickness though.
Enlarge the sheetmetal holes for the steering bronze bushings. Radial positioning of these bushings is irrelevant. No need to have press-fits on an obnoxious weldment.
the lift motor is sloppy. If you tighten it it's much better but still kinda sloppy. Remember this is tapped into a .09" thick wall tube... So tightening scares me a bit