Last Sync: 2025-10-10 11:13 (Mobile)
This commit is contained in:
6
.obsidian/workspace-mobile.json
vendored
6
.obsidian/workspace-mobile.json
vendored
@@ -27,12 +27,12 @@
|
|||||||
"state": {
|
"state": {
|
||||||
"type": "markdown",
|
"type": "markdown",
|
||||||
"state": {
|
"state": {
|
||||||
"file": "stockcropper/Notes from assembly 13SEP2025.md",
|
"file": "stockcropper/SC-PUNCHLIST.md",
|
||||||
"mode": "source",
|
"mode": "source",
|
||||||
"source": false
|
"source": false
|
||||||
},
|
},
|
||||||
"icon": "lucide-file",
|
"icon": "lucide-file",
|
||||||
"title": "Notes from assembly 13SEP2025"
|
"title": "SC-PUNCHLIST"
|
||||||
}
|
}
|
||||||
}
|
}
|
||||||
],
|
],
|
||||||
@@ -167,8 +167,8 @@
|
|||||||
},
|
},
|
||||||
"active": "0b023202c927812b",
|
"active": "0b023202c927812b",
|
||||||
"lastOpenFiles": [
|
"lastOpenFiles": [
|
||||||
"stockcropper/SC-PUNCHLIST.md",
|
|
||||||
"stockcropper/Notes from assembly 13SEP2025.md",
|
"stockcropper/Notes from assembly 13SEP2025.md",
|
||||||
|
"stockcropper/SC-PUNCHLIST.md",
|
||||||
"10Oct2025.md",
|
"10Oct2025.md",
|
||||||
"Shop Rate.md",
|
"Shop Rate.md",
|
||||||
"09Oct2025.md",
|
"09Oct2025.md",
|
||||||
|
|||||||
@@ -1,22 +1,11 @@
|
|||||||
•
|
• Jack nut pressed in really tight. Loosen this a bit if at all possible. It made the threads jam up. I re-tapped the threads after pressing it in. It didn’t press in all the way (about 1/16” didn’t go in) but the flange also wasn’t quite to spec so this is a good representation.
|
||||||
Jack nut pressed in really tight. Loosen this a bit if at all possible. It made the threads jam up. I re-tapped the threads after pressing it in. It didn’t press in all the way (about 1/16” didn’t go in) but the flange also wasn’t quite to spec so this is a good representation.
|
• Everything went on the axle tighter than desired. Maybe this should be undersized.
|
||||||
•
|
• The main axle is too long for the pins to latch over. I think it was fabricated wrong… double check this. We just elongated the clips on the pins for now.
|
||||||
Everything went on the axle tighter than desired. Maybe this should be undersized.
|
• I sanded out the bores for the main axle bushings. This didn’t take long. This is probably the right thing to do - don’t even change the nominal hole size, just sand to a nice tight slip fit.
|
||||||
•
|
• The main tube would go on easier if it just bottomed out against the bushing. Just do it. Or slot the sheetmetal. Do something so this is easy.
|
||||||
The main axle is too long for the pins to latch over. I think it was fabricated wrong… double check this. We just elongated the clips on the pins for now.
|
• Maybe you should make the towbar telescope!
|
||||||
•
|
• The drive motor purchased had M8 threads. It also didn’t need the spacers (spacing was perfect already!). It just needed the shaft cut down. Verify what you’re working with.
|
||||||
I sanded out the bores for the main axle bushings. This didn’t take long. This is probably the right thing to do - don’t even change the nominal hole size, just sand to a nice tight slip fit.
|
• Need to chase / retap the M12x1 nuts after welding (and prior to painting).
|
||||||
•
|
• You didn’t order or make the steering handle. Robbed part from THF. It’s not the right thickness though.
|
||||||
The main tube would go on easier if it just bottomed out against the bushing. Just do it. Or slot the sheetmetal. Do something so this is easy.
|
• Enlarge the sheetmetal holes for the steering bronze bushings. Radial positioning of these bushings is irrelevant. No need to have press-fits on an obnoxious weldment.
|
||||||
•
|
• The lift motor is sloppy. If you tighten it it's much better but still kinda sloppy. Remember this is tapped into a .09" thick wall tube... So tightening scares me a bit
|
||||||
Maybe you should make the towbar telescope!
|
|
||||||
•
|
|
||||||
The drive motor purchased had M8 threads. It also didn’t need the spacers (spacing was perfect already!). It just needed the shaft cut down. Verify what you’re working with.
|
|
||||||
•
|
|
||||||
Need to chase / retap the M12x1 nuts after welding (and prior to painting).
|
|
||||||
•
|
|
||||||
You didn’t order or make the steering handle. Robbed part from THF. It’s not the right thickness though.
|
|
||||||
•
|
|
||||||
Enlarge the sheetmetal holes for the steering bronze bushings. Radial positioning of these bushings is irrelevant. No need to have press-fits on an obnoxious weldment.
|
|
||||||
•
|
|
||||||
the lift motor is sloppy. If you tighten it it's much better but still kinda sloppy. Remember this is tapped into a .09" thick wall tube... So tightening scares me a bit
|
|
||||||
Reference in New Issue
Block a user