Last Sync: 2025-10-10 11:13 (Mobile)
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Jack nut pressed in really tight. Loosen this a bit if at all possible. It made the threads jam up. I re-tapped the threads after pressing it in. It didn’t press in all the way (about 1/16” didn’t go in) but the flange also wasn’t quite to spec so this is a good representation.
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Everything went on the axle tighter than desired. Maybe this should be undersized.
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The main axle is too long for the pins to latch over. I think it was fabricated wrong… double check this. We just elongated the clips on the pins for now.
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I sanded out the bores for the main axle bushings. This didn’t take long. This is probably the right thing to do - don’t even change the nominal hole size, just sand to a nice tight slip fit.
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The main tube would go on easier if it just bottomed out against the bushing. Just do it. Or slot the sheetmetal. Do something so this is easy.
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Maybe you should make the towbar telescope!
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The drive motor purchased had M8 threads. It also didn’t need the spacers (spacing was perfect already!). It just needed the shaft cut down. Verify what you’re working with.
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Need to chase / retap the M12x1 nuts after welding (and prior to painting).
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You didn’t order or make the steering handle. Robbed part from THF. It’s not the right thickness though.
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Enlarge the sheetmetal holes for the steering bronze bushings. Radial positioning of these bushings is irrelevant. No need to have press-fits on an obnoxious weldment.
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•
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the lift motor is sloppy. If you tighten it it's much better but still kinda sloppy. Remember this is tapped into a .09" thick wall tube... So tightening scares me a bit
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• Jack nut pressed in really tight. Loosen this a bit if at all possible. It made the threads jam up. I re-tapped the threads after pressing it in. It didn’t press in all the way (about 1/16” didn’t go in) but the flange also wasn’t quite to spec so this is a good representation.
|
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• Everything went on the axle tighter than desired. Maybe this should be undersized.
|
||||
• The main axle is too long for the pins to latch over. I think it was fabricated wrong… double check this. We just elongated the clips on the pins for now.
|
||||
• I sanded out the bores for the main axle bushings. This didn’t take long. This is probably the right thing to do - don’t even change the nominal hole size, just sand to a nice tight slip fit.
|
||||
• The main tube would go on easier if it just bottomed out against the bushing. Just do it. Or slot the sheetmetal. Do something so this is easy.
|
||||
• Maybe you should make the towbar telescope!
|
||||
• The drive motor purchased had M8 threads. It also didn’t need the spacers (spacing was perfect already!). It just needed the shaft cut down. Verify what you’re working with.
|
||||
• Need to chase / retap the M12x1 nuts after welding (and prior to painting).
|
||||
• You didn’t order or make the steering handle. Robbed part from THF. It’s not the right thickness though.
|
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• Enlarge the sheetmetal holes for the steering bronze bushings. Radial positioning of these bushings is irrelevant. No need to have press-fits on an obnoxious weldment.
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• The lift motor is sloppy. If you tighten it it's much better but still kinda sloppy. Remember this is tapped into a .09" thick wall tube... So tightening scares me a bit
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